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HomeMy WebLinkAbout851193.tiff rJC`EOP RECV(,r UNITED STATES O '"4 NUCLEAR REGULATORY COMMISSION ° i; REGION IV Ill RYAN PLAZA DRIVE,SUITE 1000 °cs� N°‘� ARLINGTON,TEXAS 78011 AUG 2 8 1985 Docket: 50-267 p••tn noire pruq�nnn��S Public Service Company of Colorado } 1 ATTN: M. Holmes, Licensing Manager SEP 3 1985 I P. 0. Box 840 Denver, Colorado 80201-0840 GzeeLer. cow. Gentlemen: As we discussed during the meeting on Technical Specifications (TSs) at the Fort St. Vrain Station on July 26, 1985, and during the telephone conference on August 13, 1985, it is our intention to include the review and approval of some of the applications for proposed changes to the TSs as part of the Upgrade Program. Attached as Enclosures 1 and 2 are the lists of applications which we intend to review as part of the Upgrade Program and those we intend to review separately. It is our present opinion that the applications included in Enclosure 1 are not completely acceptable and would require some modification; the comparable requirements in the Upgrade Program draft, however, appear to be more acceptable. Therefore, it appears that a more efficient use of your and our resources can be achieved by incorporating certain reviews into the Upgrade Program. I would appreciate your review of the enclosures to ensure the accuracy and completeness of the pending applications and any comments you may have on our approach. Sincerely, yLae C Philip C. Wagner Senior Project Manager Enclosures: As stated cc: Mr. D. W. Warembourg, Manager Nuclear Engineering Division Public Service Company of Colorado P. 0. Box 840 Denver, Colorado 80201 851193 -2- Mr. David Alberstein, 14/159A GA Technologies, Inc. P. O. Box 85608 San Diego, California 92138 Kelley, Stansfield & O'Donnell Public Service Company Building 550 15th Street, Room 900 Denver, Colorado 80202 Chairman, Board of County Comm. of Weld County, Colorado Greeley, Colorado 80631 Regional Representative Radiation Programs Environmental Protection Agency 1860 Lincoln Street Denver, Colorado 80203 Mr. H. L. Brey, Manager Nuclear Licensing/Fuels Div. Public Service Company of Colorado P. O. Box 840 Denver, Colorado 80201 J. W. Gahm, Manager, Nuclear Production Division Fort St. Vrain Nuclear Station 16805 WCR 19} Platteville, Colorado 80651 L. Singleton, Manager, Quality Assurance Division (same address) Colorado Radiation Control Program Director Enclosure 1 ACTIONS TO BE INCLUDED IN THE TECHNICAL SPECIFICATION UPGRADE PROGRAM 1. Electrical Technical Specifications (TAC 51955) - The original application (P-83415) dated 12/30/83, which was submitted in response to Safety Evaluations dated 8/17/82 and 10/12/82 related to degraded grid and onsite power systems undervoltage protection, was superseded by a rewrite of the electrical systems section of the TSs in response to a 10/12/83 enforcement conference commitment. The 6/26/84 (P-84187) reapplication did not contain all of the requested upgrades and was further revised by a 2/6/85 (P-85041) application. (This application also responds to Generic Letter 84-15 (TAC 55861) for diesel generator reliability.) - Since the latest submittal is not completely acceptable and since recent NRC positions of diesel generator testing appear to be more acceptable to PSC, the needed revisions will be included in the Upgrade Program and no further action will be taken on the submitted applications. - The recently completed modifications to the AC and DC electrical systems are being reviewed for acceptability as a separate issue. 2. NUREG-0737 Technical Specifications (TAC 54535) - The application dated 7/31/84 (P-84242) was submitted in response to Generic Letters 83-36 and 37. Review of the Upgrade Program draft indicates that the requirements contained therein more closely follow the guidance contained in the Generic Letters than the proposed application. Therefore, inclusion of this review in the Upgrade Program seems to be appropriate. 3. Circulator Operability Requirements (TAC 56927) - The application dated 2/6/85 (P-85042) would require numerous changes to be found acceptable. The requirements proposed in the Upgrade Program are being revised as a result of the meetings conducted from July 22 to 26, 1985. Therefore, efficiency would indicate that his application should be included in the Upgrade Program. 4. Restart Requirements - The tendon wire surveillance requirements approved in the July 8, 1985 Safety Evaluation will be included in the Upgrade Program as committed to by PSC. - The revised interim Control Rod Drive Mechanism and Reactivity Control Technical Specifications approved in Safety Evaluations dated July 12, 1985 and July 23, 1985, will be included in the Upgrade Program as committed to by PSC. Enclosure 2 ACTIONS BEING REVIEWED INDEPENDENTLY 1 Instrument Setpoints (TAC 47416) - Problems discovered in the methods used to establish instrument setpoints resulted in a 10/1/80 applications which was discussed at a meeting in Denver on 10/27/83 during which PSC agreed to a resubmittal . The reapplication provided by letter dated 6/21/85 (P-85214) is being reviewed by NRR under TIA 83-15. - The recent application contains some accident reanalyses which will require review in addition to the instrumentation review. Present plans call for completing our review in a time frame to allow incorporation into the Upgrade Program, however, due to the magnitude of this review effort, a contingency plan to use existing values in the Upgrade at the time of issuance should be developed. 2. L.C.O. 4.1.9 (TAC 52634) - Following the discovery of nonconservative assumptions in establishing these power-to-flow requirements 10/11/83, PSC submitted an LER com- mitting to follow conservative guidance and provide a corrected require- ment. An application dated 12/15/83 (P-83403) was reviewed and determined to be unacceptable. Meeting between us, our consultant at ORNL and PSC (see summary dated 9/6/84) have not resulted in a revised application. ORNL guidance on 7/17/85 and PSC submittal 8/1/85 (P-85271) indicate progress is being made. - This issue should be resolved in the near future with the result then included in the Upgrade Program. It may be appropriate for another meeting among all involved parties to reach final resolution prior to the commitment of including the new requirements in the 10/15/85 Upgrade submittal . 3. ISI/IST Requirements (TAC 53417) - The 12/30/83 (P-83416) application was submitted in response to commitments to include appropriate requirements in the TSs. The preliminary results of our review were discussed during site meetings on July 22 to 26, 1985. The results of our review and the meeting discussions will be transmitted to PSC in the near future. - We have determined that these inspection and testing requirements should not be delayed until completion of the Upgrade Program and we will review the resubmittal PSC committed to submit within 90 days of their receipt of our evaluation as a separate issue. 4. Circulator Overspeed Trip Setpoint (TAC 55052) - The application dated 5/10/84 (P-84137) contained insufficient justifi- cation to allow a compete review. A response to the 10/25/84 questions was submitted by letter dated 12/27/84 (P-84537). A request for NRR review assistance was made by memo (Denise to Eisenhut) dated 1/28/85. -2- - Since this change will have little effect on the Uprade Program, the review is being handled separately. 5. Organizational Changes (TAC 56743) - The 1/14/85 (P-85009) application was determined to be obsolete prior to the expiration of the notice period and a revised set of requirements was submitted by application dated 6/10/85 (P-85155). The revised application, however, includes a reference to the Fuel Surveillance Program which was submitted by letter dated 5/3/85 (P-85151). - Prior to the approval of the revised application, it will be necessary for NRC to accept the Fuel Surveillance Program as incorporating all of the past commitments and agreements on this subject. This review should be completed in the near future so the organizational changes can be approved and issued to reestablish compliance with the TS. 6. Xenon Stability Testing (TAC 57788) - In order to complete the initial rise-to-power testing program item on xenon stability, it is necessary to allow a temporary change to the TS requirement on control rod position. A special test exception type change was proposed on 5/22/85 (P-85179). - In order to allow completion of the test program during Cycle 4 (see P-85063 dated 3/5/85 for the PSC commitment to complete these tests) this change needs to be processed as a separate issue. UNITED STATES WELD GOIivTY Cpbmk7lSe!n,-; DEPARTMENT OF THE INTERIOR Q ^ `! -'7a17' BUREAU OF RECLAMATION LOWER MISSOURI REGION SEP 3 1985 UPPER COLORADO REGION 'GREELEY, COLO. NOTICE OF INITIATION OF INVESTIGATIONS Name of Investigation: High Mountain Aquifer Study, Colorado Type of Investigation: Special Location of Investigation: Scattered throughout the high mountain areas of the State of Colorado are 71 potential glacial • aquifer sites. For the most part these sites are in close proximity to the Continental Divide. Date Investigation Initiated: Investigation will be initiated in fiscal year 1985. The study will culminate in January of 1990 with a Special Report which will present the study findings. 1. Scope of Investigation: The primary purpose of this study is to determine the possibility of using the glacial aquifers as storage reser- voirs. If these basins can be used as storage reservoirs, they would collect water from snowmelt and rainfall and release it when downstream demands are high. Two advantages anticipated from using glacial aquifers are a reduction in evaporation losses and a savings of capital cost for constructing surface storage reservoirs. Environmental and social impacts of aquifer storage may also prove to be fewer than those associated with surface storage reservoirs. This study will evaluate the technical aspects of using these glacial aquifers as storage reservoirs. It is not intended to reach full-scale development of any high mountain aquifer. Hydrologic studies, engineering cost estimates, and economic and environmental evaluations will be made to determine if these sites compare favorably with other sources of water supplies and storage. The study will also look at the legal constraints involved and their effect on this type of development. The resolving of state water rights issues will not be a part of this study effort. 2. Problem: The water supplies in Colorado for irrigation, municipal , and industrial uses are becoming more scarce and expensive to develop. The use of high mountain glacial aquifers as storage reservoirs may prove to be a more economical , efficient, and environmentally acceptable way to develop and manage Colorado' s water resources. 3. Prospective Solutions: The 71 potential sites are mostly found above the 8500 foot elevation and have an average elevation of just over 9000 feet. They vary in size from about 100 to 2,000 acres. As a storage facility, the basins would capture water at a time of high flow and release water when a dependable water supply is needed downstream. These glacial aquifers may also be developed for replacement and/or compensatory storage for the movement of water from one tributary basin to another. These water transfers could be entirely on one side of the Continental Divide, or involve a transmountain diversion. 4. Participation: The Bureau of Reclamation and the CORY Company, Inc. , a private entity, signed a contract on August 21, 1984, to share the cost of this investigation. Other interested entities include the State of Colorado and the Colorado delegation, the Colorado Water Conservation Board, the Colorado State Engineer, the Colorado River Water Conservation District, and the West Divide Water Conservancy District. The Forest Service and the Fish and Wildlife Service have been notified of upcoming study activities. Meetings have been held with 10 of the major water orga- nizations in the State to advise them of the proposed investigations and to exchange information. 5. Indication of interest: Expressions of interest should be sent to: East Slope West Slope Bureau of Reclamation Bureau of Reclamation Lower Missouri Region Upper Colorado Region PO Box 25247 PO Box 2553 Building 20, Denver Federal Center 125 S. State Street Denver, CO 80225-0247 Salt Lake City, UT 84147 (Attention: William J. Steele (Attention: Harl Noble Regional Planning Officer Regional Planning Officer 303-236-0489) 801-524-5517) Prepared: August 1 , 1985 Transmitted: August 30, 1985 . % a , 27/- Regional Plann�hg Officer Regional Planning 0 ficer Lower Missouri egion Upper Colorado Region ACTINCaRe iol Director `� ds!?alte g � eg onal Directo Lower Missouri Region Upper Colorado Region SSINS No. : 6835 IN 85-75 W'E�LDD COUNTY COMMISS!us UNITED STATES NUCLEAR REGULATORY COMMISSION o E 4EIn c1L c fa OFFICE OF INSPECTION AND ENFORCEM� � �! WASHINGTON, D.C. 20555 SEP 5 1985 ' Li August 30, 1985 IE INFORMATION NOTICE NO. 85-75: IMPROPERLY INSTALLED INSTRUMENTATION, INADEQUATE QUALITY CONTROL AND INADEQUATE POSTMODIFICATION TESTING Addressees: All nuclear power reactor facilities holding an operating license (OL) or a construction permit (CP). Purpose: This information notice is to alert addressees of two recent instances of improper system modifications, inadequate quality control and inadequate post- modification testing following installation of environmentally qualified equipment. Recipients are expected to review the information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements; therefore, no specific action or written response is required. Description of Circumstances: LaSalle Unit 2 On June 10, 1985, at 11: 30 a.m. , the licensee informed the NRC Resident Inspector that for approximately 5 days LaSalle Unit 2 had been without the capability of automatic actuation of emergency core cooling (ECCS) and that for approximately 3 days during this period the plant had been without secondary containment integrity. The major cause of this condition was improper installation (the variable and reference legs were reversed) of the two reactor vessel level actuation switches which control Division I automatic depressurization system (ADS) , low pressure core spray (LPCS), and reactor core isolation cooling (RCIC). Unit 2 was shut down in February 1985 for an outage that included installation of environmentally qualified electrical equipment. LaSalle has three divisions of ECCS equipment. In March 1985, ECCS Division III was taken out of service for maintenance. On June 5, 1985, ECCS Division II was taken out of service for modifications. On June 3, 1985, secondary containment was declared inoperable for maintenance on the reactor building ventilation system. The result of these scheduled actions was that two of three ECCS divisions and secondary containment were inoperable, leaving ECCS Division I available for use. Subsequently, it was discovered that the variable and reference legs to the 8508270286 IN 85-75 August 30, 1985 Page 2 of 3 reactor vessel level actuation switches for ECCS Division I had been accidentally reversed since June 3, 1985; thus leaving the plant with no ECCS automatic actuation and no secondary containment. The cause of the piping reversal was initially the result of incorrect design drawings which were released to the contractor on April 1, 1985. The licensee's site personnel recognized the error on April 4, 1985, and issued a Field Change Request to correct it. However, the isometric drawings being used at the location of the modification activities were not corrected. Therefore, the contractor proceeded to connect piping in the reverse order from the correct configuration. Figure 1 shows the correct configuration and Figure 2 shows the reversal . This error was not identified by the Quality Control (QC) Program because the contractor' s QC did not assign inspection hold points for either the electrical or mechanical piping connections for any of the 22 instruments replaced by the modification. Consequently, the installation adequacy was not verified against the design drawings, which did include the field change and, therefore, which could reasonably be expected to have revealed the error in the two instruments that were piped backwards. Subsequent postmodification testing failed to detect the error because (as shown in Figure 3) the test shut the instrument block isolation valves and injected a test pressure source through the installed test connections downstream from the instrument. This test method isolated the portion of the piping where the reversal occurred from the test because it was upstream of the shut valves. The error was found as a result of a fortuitous observation by an instrument technician who was performing an unrelated test. If this technician had not noticed the error, there was a significant possibility that the plant would have operated with one division of ECCS unavailable. The safety significance of these events was reduced because the plant was in a cold shutdown condition. However, no ECCS equipment was available for automatic operation in the event of low reactor vessel level . In addition, secondary containment was allowed to be relaxed because the licensee believed ECCS Division I was operable. Primary containment also was open. Consequently, had a leak occurred, no ECCS systems would have functioned automatically and secondary containment would not have been available either. Technical specifications required the operability of some ECCS equipment during the time that the plant was shutdown, and upon loss of ECCS, secondary containment integrity was subsequently required. Trojan On July 20, 1985, the Trojan Nuclear Power Plant tripped from 100% power because of a turbine trip that was caused by the loss of the unit auxiliary transformer. All systems functioned normally except that low suction pressure caused one auxiliary feedwater pump to trip and then the other auxiliary feedwater pump to trip after restart of the first auxiliary feedwater pump. IN 85-75 August 30, 1985 Page 3 of 3 The cause of the trips of the auxiliary feedwater pumps can be traced back to improper postmodification adjustment and inadequate postmodification testing following retrofit of environmentally qualified controllers for the auxiliary feedwater system. The auxiliary feedwater pump trips on low suction pressure were caused by excessive combined flow from the two auxiliary feedwater pumps that draw from a single header from the condensate storage tank. The flow control valves were open farther than required after new environmentally qualified controllers had been installed during a recent refueling outage. When the flow control valves were adjusted following the modification of the controllers, only one auxiliary feedwater pump was run at a time and used to adjust the control valve limit switch settings. Consequently, when both pumps were started following the reactor trip on July 20, 1985, the combined flow was excessive. Discussion: Information Notice 85-23, "Inadequate Surveillance and Postmaintenance and Postmodification System Testing," described a series of events occurring at McGuire in November of 1984, where improper system modifications and inadequate postmodification testing also were involved. No specific action or written response is required by this information notice. If you have any questions about this matter, please contact the Regional Administrator of the appropriate regional office or this office. dward ordan, Director Divisi of Emergency Preparedness and ngineering Response Office of Inspection and Enforcement Technical Contacts: Eric Weiss, IE (301) 492-9005 M. Jordan, SRI, LaSalle (815) 357-8611 Robert Dodds, Region V (415) 943-3720 Attachments: 1. Figures Illustrating LaSalle Level Instrument Problems 2. List of Recently Issued IE Information Notices nttachnent 1 IN 85-75 August 3C, 1985 REFERENCE REFERENCE REACTOR REACTOR PRESSURE PRESSURE VESSEL VESSEL VARIABLE VARIABLE A A A A INSTRUMENT INSTRUMENT BLOCK _ - BLOCK i--- r I I I I• • I♦ A A A LOW LIS HIGH LOW LIS HIGH Figure 1 Figure 2 REFERENCE REACTOR PRESSURE VESSEL VARIABLE V A A INSTRUMENT BLOCK r-- I I CLOSED CLOSED ---1 OPEN CLOSED CLOSED LOW LIS HIGH (OPEN) U I TEST DEVICE Figure 3 Attachment 2 IN 85-75 August 30, 1985 LIST OF RECENTLY ISSUED IE INFORMATION NOTICES Information Date of Notice No. Subject Issue Issued to 85-74 Station Battery Problems 8/29/85 All power reactor facilities holding an OL or CP 84-70 Reliance On Water Level 8/26/85 All power reactor Sup. 1 Instrumentation With A facilities holding Common Reference Leg an OL or CP 85-73 Emergency Diesel Generator 8/23/85 All power reactor Control Circuit Logic Design facilities holding Error an OL or CP 85-72 Uncontrolled Leakage Of 8/22/85 All power reactor Reactor Coolant Outside facilities holding Containment an OL or CP 85-71 Containment Integrated Leak 8/22/85 All power reactor Rate Tests facilities holding an OL or CP 85-70 Teletherapy Unit Full 8/15/85 All material Calibration And Qualified licensees Expert Requirements (10 CFR 35.23 And 10 CFR 35. 24) 85-69 Recent Felony Conviction For 8/15/85 All power reactor Cheating On Reactor Operator facilities holding Requalification Tests an OL or CP 85-68 Diesel Generator Failure At 8/14/85 All power reactor Calvert Cliffs Nuclear facilities holding Station Unit 1 an OL or CP 85-42 Loose Phosphor In Panasonic 8/12/85 Materials and fuel Rev. 1 800 Series Badge Thermo- cycle licensees luminescent Dosimeter (TLD) Elements 85-67 Valve-Shaft-To-Actuator Key 8/8/85 All power reactor May Fall Out Of Place When facilities holding Mounted Below Horizontal Axis an OL or CP OL = Operating License CP = Construction Permit SSINS No. : 6835 IN 85-74 UNITED STATES WELD CrIPIY r,11MlSS!P FTIS NUCLEAR REGULATORY COMMISSION -� OFFICE OF INSPECTION AND ENFORCEMENT DE FIT WASHINGTON, DC 20555 SEP 51985 ,` August 29, 1985 GRELLEY, CO'._O. IE INFORMATION NOTICE NO. 85-74: STATION BATTERY PROBLEMS Addressees: All nuclear power reactor facilities holding an operating license (OL) or a construction permit (CP). Purpose: This notice describes problems that have occurred with lead-acid station batteries at several nuclear power plants. These problems were discovered as a result of inspections by the NRC Performance Appraisal Team (PAT). It is expected that recipients will review the information for applicability to their facilities and consider actions, if appropriate, to preclude a similar problem occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements; therefore, no specific action or written response is required. Description of Circumstances: All four recent inspections by the PAT identified problems with lead-acid station batteries. Although all of the problems are not listed here, a summary of a few of the more significant problems with lead-acid station batteries that were identified as a result of these inspections is provided below: Cooper PAT Inspection (November 1984): The battery rated-load discharge test was performed at a discharge rate significantly less than the manufacturer' s recommended rated-load discharge rate for the 8-hour period of the test. The licensee had no records of battery charging following the completion of battery discharge test and consequently the time and date the batteries were returned to service could not be determined. The licensee failed to correct specific gravity measurements for electrolyte temperature and level . The licensee had no written procedures for conducting charges of the station batteries. McGuire PAT Inspection (February 1985): Three cells were placed on single-cell chargers for about 2 years, thus raising questions regarding the operability of the battery and electrical independence and separation of the Class 1E dc power systems. The cells on single cell 8508270031 - - IN 85-74 August 29, 1985 Page 2 of 3 charge were at voltages higher than specified in the vendor manual . Although one cell in the battery was jumpered out, the float voltage for the entire battery was not reduced; consequently each cell was floated at a voltage higher than specified in the battery vendor manual . The battery performance discharge test was performed improperly because the test was stopped before reaching the minimum specified voltage. Susquehanna PAT Inspection (February 1985): There were no station procedures for maintaining station batteries in accordance with the battery vendor' s manual or IEEE Std 450-1975, "IEEE Recommended Practice for Maintenance, Testing and Replacement of Large Lead Storage Batteries for Generating Stations and Substations" (which is endorsed by Regulatory Guide 1. 129, "Maintenance, Testing and Replacement of Large Lead Storage Batteries for Nuclear Power Plants"). Intercell resistance values were not compared with previous values to determine when corrective action was required. The licensee did not always conduct equalizing charges when required; nor did the licensee have procedures for monitoring the progress of an equalizing charge or determining when the charge should be terminated. Surveillance procedures for the 60-month rated-capacity discharge test did not conform to IEEE Std 450-1975 because the test was terminated at the end of 8 hours, instead of when the terminal voltage fell to the minimum specified value (usually 1.75 volts per cell). The licensee' s procedures did not require that the average specific gravity be calculated and compared to the technical specification acceptance criteria. San Onofre PAT Inspection (March 1985): During the first 2 years of operation, the battery capacity tests required by the Final Safety Analysis Report (FSAR) and IEEE Std 450-1980 were not performed on Units 2 and 3. The total battery float voltage was not adjusted to account for two jumpered out cells. The two jumpered out cells did not receive the manufacturer' s specified surveillances, maintenance, or charges. The pilot cells were not being changed on a yearly basis, as recommended by the vendor' s technical instructions. The station engineer responsible for the technical aspects of battery operation, maintenance, and surveillance did not receive surveillance results and data sheets on a routine basis. Discussion: Recent IE inspections of operating facilities indicate that several widespread deficiencies may exist in the operation and maintenance of station batteries. These deficiencies are attributable to a variety of causes, including licensee error, inadequate knowledge of batteries by maintenance technicians and supervisors, and inadequate procedural guidance. The results of these inspections suggest a general lack of appreciation amongst licensee personnel for proper maintenance and surveillance of station batteries. Although batteries contain no moving parts, considerable care and attention to detail is required to maintain them operable. Too often, licensees may be treating these vital engineered safety features (ESF) power supplies as "passive" components and not providing them the necessary management and technical attention. IN 85-74 August 29, 1985 Page 3 of 3 The following reference materials provide guidance as to the individual requirements for a facility' s station batteries. 1. IEEE 450-1975, and 1980 2. Regulatory Guide 1.129, Rev. 1, "Maintenance, Testing and Replacement of Large Lead Storage Batteries for Nuclear Power Plants" (This regulatory guide endorses IEEE Std 450-1975 with certain exceptions. ) 3. Facility Technical Specifications 4. Final Safety Analysis Report (FSAR) 5. Station Battery Vendor Technical Manual (The vendors of station batteries periodically update their manuals to include revised guidance. ) Other recent problems with station batteries were described in IE Information Notice 84-83: VARIOUS BATTERY PROBLEMS, November 14, 1984. No specific action or written response is required by this information notice. If you have questions about this matter, please contact the Regional Adminis- trator of the appropriate NRC regional office or this office. s/I-'--- ar Jordanor Divisi of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement CONTACTS: E. W. Weiss, IE (301) 492-9005 L. J. Callan, IE (301) 492-9497 Attachment: List of Recently Issued IE Information Notices Attachment 1 IN 85-74 August 29, 1985 LIST OF RECENTLY ISSUED IE INFORMATION NOTICES Information Date of Notice No. Subject Issue Issued to 84-70 Reliance On Water Level 8/26/85 All power reactor Sup. 1 Instrumentation With A facilities holding Common Reference Leg an OL or CP 85-73 Emergency Diesel Generator 8/23/85 All power reactor Control Circuit Logic Design facilities holding Error an OL or CP 85-72 Uncontrolled Leakage Of 8/22/85 All power reactor Reactor Coolant Outside facilities holding Containment an OL or CP 85-71 Containment Integrated Leak 8/22/85 All power reactor Rate Tests facilities holding an OL or CP 85-70 Teletherapy Unit Full 8/15/85 All material Calibration And Qualified licensees Expert Requirements (10 CFR 35.23 And 10 CFR 35.24) 85-69 Recent Felony Conviction For 8/15/85 All power reactor Cheating On Reactor Operator facilities holding Requalification Tests an OL or CP 85-68 Diesel Generator Failure At 8/14/85 All power reactor Calvert Cliffs Nuclear facilities holding Station Unit 1 an OL or CP 85-42 Loose Phosphor In Panasonic 8/12/85 Materials and fuel Rev. 1 800 Series Badge Thermo- cycle licensees luminescent Dosimeter (TLD) Elements 85-67 Valve-Shaft-To-Actuator Key 8/8/85 All power reactor May Fall Out Of Place When facilities holding Mounted Below Horizontal Axis an OL or CP OL = Operating License CP = Construction Permit SSINS NO. : 6835 IN 84-70 SUPP. 1 /NEIO COOFTY Prt"t•r., ,.' UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMEN ! SEP 3 ,19 WASHINGTON, D. C. 20555 August 26, 1985 GRtE LL IE INFORMATION NOTICE NO. 84-70 SUPPLEMENT 1: RELIANCE ON WATER LEVEL INSTRUMENTATION WITH A COMMON REFERENCE LEG Addressees: All nuclear power reactor facilities holding an operating license (OL) or a construction permit (CP). Purpose: This information notice is provided to alert licensees and applicants of the potential for degradation of safety.associated with operator reliance on level instruments that share a common reference leg. In this regard, this notice supplements and reemphasizes the information contained in IE Information Notice 84-70, Reliance On Water Level Instrumentation With A Common Reference Leg. This notice serves to alert licensees and applicants to the need for operators to recognize normal and abnormal water level instrument behavior under various plant conditions. Recipients are expected to review the information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements; therefore, no specific action or written response is required. Description of Circumstances: On February 13, 1985, while performing a reactor startup at TVA' s Browns Ferry Nuclear Plant, a half scram was received on low reactor water level . A few minutes before the half scram, the operators had noticed that two of the three narrow-range General Electric measurement and control (GEMAC) water level instruments were reading approximately 40 inches of reactor vessel water level . The other narrow-range instrument was indicating approximately 10 inches of water level . Two wide-range YARWAY instruments were observed by the operators to be indicating approximately 40 inches. At the time of the half scram, reactor pressure was approximately 40 psig and reactor coolant temperature was approximately 286°F. Although four of the instruments observed by the operators indicated nearly normal reactor water level (33 ± 5 inches) , actual reactor water level was approximately 10 inches. 8508230052 IN 84-70 SUPP. 1 August 26, 1985 Page 2 of 3 The operators incorrectly concluded that the narrow-range instrument indicating 10 inches was erroneous since four other level instruments were indicating high. The two GEMAC instruments that indicated 40 inches share a common reference leg. This reference leg had lost some of its water inventory, causing all level instrumentation that tapped off that leg to erroneously indicate high. The GEMAC instrument that was reading 10 inches tapped off a different reference column than the aforementioned instruments. The two wide-range YARWAY instruments each have separate reference columns not shared by any of the narrow- range GEMAC instruments. At approximately 40 psig reactor pressure and with actual reactor water level at 33 ± 5 inches, the YARWAY instruments should indicate ?60 inches, a normal YARWAY level indication. A YARWAY level indication of 40 inches should have alerted the operators that water level was abnormally low. The operators did not check the shutdown vessel flooding range level indication which was available in the control room. This instrument would have confirmed actual low water level conditions since it is calibrated for cold plant conditions. Discussion: The cause of this event was a partial loss of water inventory from a reference leg that is common to several water level instruments, including instrument channels required by the Technical Specifications. From a reactor safety perspective, this event highlights the need for operators to be cognizant of level instruments that share a common reference leg and also to be aware of level instrument behavior subject to various plant conditions. A problem in a reference leg, such as that experienced at Browns Ferry, not only affects level indication, but may also affect the operability of reactor pro- tection instrument channels required by the Technical Specifications. In this event, the most critical technical specification instruments affected were two level switches, one in each reactor protection trip system train. These switches were inoperable since they were common to the faulty reference leg. Had the operators realized earlier what instruments and switches were affected by the faulty reference leg, proper corrective action may have been taken to shut down the plant in a timely manner in accordance with the Technical Specifications. It is important that operators understand level instrument response to various plant conditions. One way to achieve this understanding is through training to emphasize level instrument system design, temperature and/or pressure compen- sation, instrument calibration, and the purpose of the instruments (i . e. , process monitor vs. control ). Although the YARWAY instruments are designed to provide wide-range accident level indication and are calibrated to be most accurate at normal operating reactor pressure, the operators at Browns Ferry could still have used these instruments as additional level response indication. Had the operators realized that a YARWAY level of 40 inches was abnormally low for the existing low reactor pressure, they might have been alerted earlier to the fact that actual vessel water level was low. Licensees and applicants may wish to review their system descriptions, operating procedures, and operator training programs to ensure that a common reference leg shared by multiple level instruments is adequately addressed. Operator awareness of the effects a malfunction in a common reference leg can have on the level instruments and recognition of proper water level indication subject to various plant conditions can enhance plant safety. IN 84-70 SUPP. 1 August 26, 1985 Page 3 of 3 Although Information Notice 84-70 described an event at a pressurized water reactor and this supplement describes an event at a boiling water reactor, problems associated with reliance on water level instrumentation with a common reference leg can occur at either type of reactor. No specific action or written response is required to this information notice. If you need additional information about this matter, please contact the Regional Administrator of the appropriate NRC regional office or one of the technical contacts listed below. lrd . Jordan, Director Divisi of Emergency Preparedness and gineering Response Office of Inspection and Enforcement Technical Contacts: Eric W. Weiss, IE (301) 492-9005 P. D. Wagner, Region II (404) 221-2688 Attachment: List of Recently Issued IE Information Notices Attachment 1 IN 84-70 Supp. 1 August 26, 1985 LIST OF RECENTLY ISSUED IE INFORMATION NOTICES Information Date of Notice No. Subject Issue Issued to 85-73 Emergency Diesel Generator 8/23/85 All power reactor Control Circuit Logic Design facilities holding Error an OL or CP 85-72 Uncontrolled Leakage Of 8/22/85 All power reactor Reactor Coolant Outside facilities holding Containment an OL or CP 85-71 Containment Integrated Leak 8/22/85 All power reactor Rate Tests facilities holding an OL or CP 85-70 Teletherapy Unit Full 8/15/85 All material Calibration And Qualified licensees Expert Requirements (10 CFR 35.23 And 10 CFR 35. 24) 85-69 Recent Felony Conviction For 8/15/85 All power reactor Cheating On Reactor Operator facilities holding Requalification Tests an OL or CP 85-68 Diesel Generator Failure At 8/14/85 All power reactor Calvert Cliffs Nuclear facilities holding Station Unit 1 an OL or CP 85-42 Loose Phosphor In Panasonic 8/12/85 Materials and fuel Rev. 1 800 Series Badge Thermo- cycle licensees luminescent Dosimeter (TLD) Elements 85-67 Valve-Shaft-To-Actuator Key 8/8/85 All power reactor May Fall Out Of Place When facilities holding Mounted Below Horizontal Axis an OL or CP 85-66 Discrepancies Between 8/7/85 All power reactor As-Built Construction facilities holding Drawings And Equipment an OL or CP Installations OL = Operating License CP = Construction Permit Enclosure EVALUATION OF TECHNICAL SPECIFICATION CHANGES FOR INSERVICE INSPECTION AND TESTING PROPOSED ON DECEMBER 30, 1983 PUBLIC SERVICE COMPANY OF COLORADO FORT ST. VRAIN NUCLEAR GENERATING STATION DOCKET 50-267 INTRODUCTION By letter dated December 30, 1983 (Reference 1) the Public Service Company of Colorado (PSC) proposed changes to the Fort St. Vrain Technical Specifications concerning inservice inspection and testing requirements (ISIT). These proposed changes are a continuation of the ISIT upgrade program initiated in response to a commitment in Section 3.3 of the Safety Evaluation Report of January 20, 1972 (Reference 2) to review the in-service inspection program five years following the start of commercial operation. The NRC and PSC agreed to a staged and prioritized upgrade program with those systems of highest priority identified as Category I (Reference 3). Our reviews and revisions of essentially all the Category I systems were issued on March 8, 1983 (Reference 4) as License Amendment No. 33 together with a supporting Safety Evaluation Report. Reference 1 addresses a single Category I surveillance interval and certain Category II and III changes but does not complete the upgrade program. We used the ASME Boiler and Pressure Vessel - 2 - Code, Section XI , Division 2, "Rules for Inspection and Testing of Components of Gas Cooled Reactors," as guidance in performing our review. This was in addition to our usual custom review practice for Fort St. Vrain that is based upon operating history and experience, consideration of safety importance based on safety analyses, and the unique design features of the facility. GENERAL COMMENTS 1) The NRC has not yet formally adopted Division 2, Section XI of the ASME Code. This is due to both a lack of resources for the NRC to participate in the final stages in the Code's development and to a technical concern. The technical concern pertains to Articles 1GB-1221, "Exemptions Based on Component Function," and 1223,"Exemptions Based on Component Size," which would exempt from examinations those connections to the primary system for which failure would not result in a rate of depressurization greater than that used for the design basis accident. While we believe exemptions for connections of the size of instrument lines are acceptable, as is permitted for LWRs, substantially larger sizes, and certainly those approaching the reference cross sectional area for a design basis accident should not be exempted from review. - 3 - In spite of the fact that the Division 2 Code has not been adopted by the NRC it is useful for guidance purposes in many areas of gas reactor ISIT. In the present review, changes in many surveillance requirements for safety related water systems were proposed. For this reason sections of the ASME Code dealing with pumps (Article 1GP) and valves (Article IGV) were particularly relevant to our review. In general , these sections were modeled after corresponding sections of the ASME Code for LWRs and are judged in many cases directly pertinent to inspection and testing of the safety related water systems of Fort St. Vrain. We have in the past and continue to recommend that Public Service of Colorado commit to referencing applicable sections of the Division 2 ASME Code. By reference to the Code both the presentation and the review of the inspection and testing program is expedited and many details of procedures practice are clarified. 2) As stated previously the inservice inspection upgrade program is not yet complete. In accordance with Reference 3, the following systems remain outstanding: - 4 - TABLE 1 CATEGORY II SYSTEMS CONTROL AND ORIFICE ASSEMBLY (12) NITROGEN SYSTEM (25) EMERGENCY FEED AND CONDENSATE SYSTEM (31) PURIFICATION COOLING WATER SYSTEM (47) CATEGORY III SYSTEMS FUEL STORAGE FACILITY AUXILIARY SYSTEM (14) CONTROL COMPLEX HVAC (75) FIRE PUMP HOUSE HVAC (75) AUXILIARY BOILER FUEL OIL SYSTEM (84) ESSENTIAL ELECTRIC POWER SYSTEM (92) CATEGORY IV SYSTEMS FEED AND CONDENSATE SYSTEMS (31, 32, 33) CIRCULATING WATER SYSTEM (41) DECAY HEAT REMOVAL HX (42) FIRE PROTECTION SYSTEM (45) CO2 SYSTEM (51) TURBINE STEAM SYSTEMS (52, 53, 54, 55) - 5 - TABLE 1 (Continued) RADIOACTIVE LIQUID WASTE STORAGE SYSTEM (62) RADIOACTIVE GAS WASTE SYSTEM (63) FUEL STORAGE WELL HVAC (73) PCRV ENVIRONMENT MONITORING (73) CONTROL COMPLEX ENVIRONMENT MONITORING (75) AUXILIARY BOILER (84) PRIMARY AND AUXILIARY ELECTRIC POWER SYSTEMS (92) COOLANT MEASUREMENT DISPLAY SYSTEM (93) OVERALL PLANT CONTROL SYSTEM (93) PCRV INSTRUMENTS AND DATA ACQUISITION SYSTEM (93) FAST GAS AND IODINE SAMPLING SYSTEM (93) CONTROL ROD AND ORIFICING CONTROL SYSTEM (93) SG T/C AND S/G INSTRUMENTATION SYSTEM (93) ANALYTICAL INSTRUMENTATION SYSTEM (93) The review of the surveillance requirements for these systems is expected to be accomplished mainly in the comprehensive Technical Specification Upgrade Program recently initiated by PSC (Reference 5) . This program is organizing the Technical Specifications in the general format of NRC's PWR Standard Technical Specifications. - 6 - In Reference 3 PSC provided a listing, divided into the four priority categories, of all the systems to be reviewed in the context of the 1972 commitment regarding upgraded ISIT requirements given in Reference 2. Before we can consider PSC is in compliance with its 1972 commitment PSC should review this listing, make modifications if needed, and then certify to its completeness. EVALUATION The proposed changes submitted and reviewed by this amendment action are as follows: TABLE 2 CATEGORY I SYSTEM SR 5.3.9 SAFETY VALVES SURVEILLANCE CATEGORY II SYSTEMS SR 5.2.7 WATER TURBINE DRIVE SURVEILLANCE SR 5.2.8 BEARING WATER PUMP AND MAKEUP PUMP SURVEILLANCE SR 5.2.9 HELIUM CIRCULATOR BEARING WATER ACCUMULATORS SURVEILLANCE SR 5.2.10 (b,d) FIRE WATER SYSTEM/FIRE SUPPRESSION WATER SYSTEM SURVEILLANCE SR 5.2. 16 (g) PCRV CLOSURE LEAKAGE SURVEILLANCE REQUIREMENTS SR 5.2.21 ACM TRANSFER SWITCHES, VALVES AND INSTRUMENTS SR 5.2.24 REACTOR AUXILIARY COOLING WATER SYSTEMS SURVEILLANCE SR 5.3.4 SAFE SHUTDOWN COOLING VALVES SURVEILLANCE SR 5.4.4 PCRV COOLING WATER SYSTEM TEMPERATURE INSTRUMENTS SURVEILLANCE SR 5.4.5 PCRV COOLING WATER SYSTEM FLOW INSTRUMENTS SURVEILLANCE SR 5.5.3 REACTOR BUILDING EXHAUST SYSTEM SURVEILLANCE - 7 - TABLE 2 (Continued) CATEGORY III SYSTEM SR 5.7.2 FUEL STORAGE FACILITY SURVEILLANCE Our evaluation of each of these proposed changes is stated below. 1. SR 5.2.7 - Water Turbine Drive Surveillance a) The proposed change would extend the annual test interval for one circulator and the associated water supply valving in each loop to the next scheduled plant shutdown if the test was not performed during the previous year. We find this proposed change acceptable provided that the surveillance interval does not exceed 18 months on the basis that (1) operating experience has illustrated sufficiently satisfactory performance of this system such that no significant hazard is created by an extension of this test interval , (2) potential hazards from an additional shutdown and startup transients would be avoided and (3) decay heat can still be remaved via steam driven circulators or the Liner Cooling System. The provision to not have the surveillance interval exceed 18 months is consistent with NRC Standard Technical Specifications for LWRs and ensures a minimum surveillance interval . - 8 - b) The proposed change would extend the annual test interval for safety valves in the water turbine supply lines to the next scheduled plant shutdown if the test was not performed during the previous year. We find this proposed change acceptable, provided that the surveillance interval does not exceed 18 months , based on the same reasons as given in comment 1 (a) above. c) The phrase "every three months" has been changed to read "quarterly" for the functional testing of both turbine water removal pumps and the turbine removal tank overflow to the reactor building sump. We recommend that the standard technical specification terminology of 92 days be used rather than that proposed. - 9 - 1U.1 Draft Item 4.5. 1. 1b.1 - Helium Circulator - Power Operation and Low Power The turbine water removal pumps would be tested only once per refueling cycle, an extension of the surveillance interval inconsistent with both the ASME Code and the current 92 day interval . No mention is made of surveillance of turbine water drain tank overflow. Our concerns in this regard are: (1) Why should the test interval for the turbine water removal pumps be extended to once per refueling cycle? and (2) Why is surveillance of the turbine water drain tank overflow not specified? 2. SR 5.2.8 - Bearing Water Pump and Makeup Pump Surveillance The bearing water makeup pumps have been added to this surveillance. We recommend that circulating bearing water pumps be added to the title for consistency. a) The phrase "every three months" has been changed to read "quarterly" for the operation of the Normal Makeup Pump in the recycle mode. We recommend that the terminology of STS of 92 days be used rather than that proposed. 1U indicates that this is an item from the Fort St. Vrain Technical Specification Upgrade program that corresponds to the Technical Specification under review immediately preceding. - 10 - b) Thg phrase "every three months" has been changed to read "quarterly" for the functional testing of the Emergency Makeup Pump. We recommend that the terminology of STS of 92 days be used rather than that proposed. d) The proposed surveillance for the bearing pumps would provide for a functional test of the pumps and associated instruments and controls at each scheduled plant shutdown, or at the next scheduled plant shutdown if less than a year has elapsed from the previous test. This schedule would not disrupt normal plant operation and provides a test not previously required. We find this surveillance acceptable as it is consistent with current practice in the application of the ASME Code to current plants, provided the surveillance interval does not exceed 18 months. 2U. Draft Item 4.5.1. 1.b2 - Helium Circulator - Power Operation and Low Power The bearing water makeup pump would be tested once per refueling cycle and no mention of the emergency makeup pump is made. This is incon- sistent with SR 5.2.8 and the ASME Code. In addition, no mention of bearing water pump surveillance (SR 5.2.8d) is made. Therefore, infor- mation should be provided on: (1) Why is the bearing water makeup pump surveillance inconsistent with SR 5.2.8 and the ASME Code? and (2) Why is there no surveillance requirement for the bearing water pump? - 11 - 3. SR 5.2.3 - Helium Circulator Bearing Water Accumulators The proposed test interval for testing of the helium circulator bearing water accumulators, instruments and controls would be extended from monthly to quarterly. The licensee justifies this change on a review of prior test results which shows satisfactory performance. Based on this justification we the find the proposed change acceptable. We recommend that the quarterly interval be stated as 92 days. 3U. Draft Item 4.5. 1.1.a - Helium Circulator - Power Operation and Low Power This Draft Item requires functional testing of the bearing water accumulators system at 31 day intervals but does not identify testing of the instrumentation and controls as an explicit requirement. In addition, annual calibration of the instruments is not indicated as is done in SR 5.2.9. Therefore, information should be provided addressing: (1) Why does the proposed surveillance of the accumulators omit required testing of the instrumentation and controls? and (2) Why is annual calibration not indicated? 4. SR 5.2. 10 - Fire Water System/Fire Suppression Water System Surveillance b) A reduction by 5 percent in the flow and head testing requirements for the firewater pumps has been proposed to account for pump degradation. Degradation to this degree is acceptable under the - 12 - ASME Code and the pump performance continues to exceed the minimum performance requirements by a sufficient margin. We find the proposed changes acceptable. d) The fire suppression water system pressure is changed to read "275 feet water gauge" from "125 psig." This is an acceptable change. 4U. Draft Item 4.5.4 Why does the system functional test in Part f.5 not provide for minimum flow and head measurements? To be acceptable this Draft Item should be consistent with the requirements of the ASME Code. 5. SR 5.2.16 - PCRV Closure Leakage Surveillance Requirements g) The proposed change would require once during each refueling cycle a leakage test and for each helium purification cooler well , a calibration of the well pressure monitoring instruments and a functional test of the instruments and controls used to automatically isolate the purification system. The addition of this surveillance requirement verifies the operability of instruments used to monitor containment integrity. To make a judgement on the acceptability of the proposed leakage test a description of how this requirement meets the intent of the ASME Code, Article 1GB, "Examination and Inspection," should be provided. - 13 - 5U. Draft Item 4.6.4.5.a.2 - PCRV Integrity Draft Item 4.6. 1.3 - Interspace Pressurization It is not clear that these two surveillances together contain the essential requirements of SR 5.2.16(g) . If they do not, then SR 5.2. 16(g) should be included explicitly. Alternatively, (1) each Draft Item could be modified to clarify that it pertains to "well" closures as well as "penetration" closures, or (2) a definition could be added that clarifies that a "well" closure is also a penetration closure. 6. SR 5.2.21 - ACM Transfer Switches, Valves, and Instrument Surveillance The surveillance requirement has been retitled from the previous title of SR 5.2.21 - Handvalve and Transfer Switch Surveillance. a) for those valves and transfer switches that must be manually positioned for actuation of the Alternate Cooling Method (ACM) mode of operation, the licensee proposes to change the surveillance interval to annually or at the next scheduled plant shutdown if such a test was not performed during the previous year. While we understand that full operation of these valves and switches is not possible during plant operation, we nevertheless believe that it is necessary to demonstrate operability of these components more frequently. Thus we do not find this proposed change acceptable and recommend that the original surveillance interval for an operability check of this equipment be maintained (4 to 8 months) and a full functional test be performed at annual or at refueling intervals not to exceed 18 months. - 14 - b) A new surveillance requirement for calibration at each refueling interval has been proposed for local indicators for the helium purification dryer inlet temperature, for the helium purification pumpdown line pressure and for the reactor plant cooling water surge tank cover gas pressure. From the information provided it is not clear that: (1) these proposed surveillances are sufficient to assure operational readiness of these components, and (2) the components to be given surveillance provide a complete set to assure operational readiness of the systems they serve. Therefore, infor- mation needs to be provided addressing the above. 6U. Draft Item 4.7.8.c.2 - ACM Diesel Generator This Item pertains to the surveillance of the ACM transfer switches. The proposed 18 month surveillance interval for the ACM switches is longer than the surveillance intervals proposed for these same switches in SR 5.2.21 and is not considered acceptable for the same reason and discussed in comment 6(a) above. In addition, it should be explained where the remaining surveillances have been located in the Upgrade Technical Specifications. 7. SR 5.2.24 - Reactor Auxiliary Cooling Water Systems Surveillance The title of this surveillance requirement has been changed from Circulation Water Makeup System Surveillance. We find this acceptable. - 15 - b) The surveillance interval for functionally testing each circulating water pump is proposed to be extended to monthly from weekly. As the monthly interval is in accordance with the ASME Code and surveillance requirements have been added to the proposed change regarding instrument calibration, pump performance capability and mechanical condition, we find the proposed change acceptable. d) The proposed surveillance requirement would be a new requirement pertaining to the integrity of the circulating water makeup pond embankments. The proposed addition is consistent with LWR service water requirements and is considered acceptable. e) The proposed surveillance requirement would be a new requirement pertaining to the testing of each service water pump and the associated instruments. We have reviewed these requirements and have found them in partial accord with the ASME Code. We would find them acceptable if the licensee either conforms to the detailed requirements of the ASME Code or provides an acceptable alternative. f) The proposed surveillance requirement would be a new requirement pertaining to the testing of each reactor plant cooling water pump and the associated instruments. We have reviewed these - 16 - requirements and have found them in partial accord with the ASME Code. We would find them acceptable if the licensee either conforms to the detailed requirements of the ASME Code or provides an acceptable alternative. g) The proposed surveillance requirement would be a new requirement pertaining to the testing of each purification cooling water pump and the associated instruments. We have reviewed these require- ments and have found them in partial accord with the ASME Code. We would find them acceptable if the licensee either conforms to the detailed requirements in accordance with the ASME Code or provides an acceptable alternative. h) The proposed surveillance requirement would be a new requirement pertaining to the testing and calibration of instruments and valves used for automatic insolation of portions of the reactor plant cooling water system. We find that an interval of each refueling cycle not to exceed 18 months for a full stroke test of each valve is acceptable for those valves that cannot be tested during plant operation. However, the interval for a functional check of those valves and instruments capable of being tested by a partial stroke should be performed semi-annually in accordance with the precedent of SR 5.2.21 or quarterly in accordance with the guidance of the ASME Code. - 17 - 7U. Draft Items The Draft does not recognize the Reactor Auxiliary Cooling Water System as a comprehensive system and appears to make no provisions for some of the surveillances described in SR 5.2.24. For example, in Section 4.7.4, "Service Water System" no specific surveillances are required although an operability demonstration is made by reference to surveillance testing of the diesel generators (4.8. 1. 1.2) . However, 4.8.1.1.2 has no explicit requirements pertaining to pumps, valves and instruments of this system. Specific surveillance requirements for safety systems is required by the ASME Code and should be added for the Reactor Auxiliary Cooling Water System. 8. SR 5.3.4 - Safe Shutdown Cooling Valves Surveillance The licensee proposes to test valves used for safe shutdown cooling on an annual basis or following scheduled plant shutdown. This is not acceptable except for cases where it is not physically possible to perform a more frequent surveillance. For those valves that can be tested during reactor operation, are required to initiate and function during safe shutdown cooling, and which are not called upon to operate during normal plant operation, the licensee should provide testing requirements and intervals in conformance with the ASME Code. - 18 - 8U. Draft Item 4.5.2.1.a - Steam Generator The only pertinent surveillance for valves of the safe shutdown cooling system is given by the above Draft Item which requires testing at 18 month intervals of the flow through the emergency feedwater header and the emergency condensate header to the steam generators. This is not satisfactory because it does not meet the objectives of the ASME Code which requires shorter test intervals and explicit testing procedures. The problem exists with all other Draft surveillance requirements in Section 4.5, "Safe Shutdown Cooling" as these also refer to Item 4.5.2. 1a. 9. SR 5.3.9 - Safety Valves Surveillance a) This proposed surveillance would require verification of safety valve setpoints at five year intervals for the steam generator superheater, reheater and steam/water dump tank. The requirement is satisfactory provided 1) that a schedule for additional testing is developed for any valve in a system that fails to function on a regular test and 2) that an acceptable test procedure is developed or referenced. Conformance to the ASME Code (Subsection 1GV) for Class C valve testing would meet the above requirements and simplify the development of an acceptable technical specification requirement. - 19 - b) The licensee proposed that all other Class I safety valves not covered by other surveillance requirements shall be setpoint tested at 10 year intervals. This is unacceptable. The licensee should conform with the ASME Code in this matter. 9U. Draft Item 4.5.2.1.b - Steam Generator This Item provides for setpoint testing of superheater and reheater safety valves at five year intervals but does not identify a test procedure or provide guidance in the event of testing failures. Conformance with the ASME Code would resolve this problem. Draft Item 4.7. 1.2 This Item provides a similar requirement for the steam/water pump system safety valve setpoint. Again, conformance with the ASME Code would resolve this problem. 10. SR 5.4.4 - PCRV Cooling Water System Temperature Instrument Surveillance a) The proposed surveillance requirement clarifies the monthly monitoring of the PCRV cooling system water inlet temperature, individual tube water outlet temperatures , and the associated outlet temperature alarms. We find the proposed clarification acceptable. - 20 - b) The proposed surveillance requirement clarifies requirements for annual calibration of the temperature monitoring scanner, the inlet and outlet header temperature indicators , and the outlet subheader temperature indicators. We find the proposed clarification acceptable. c) The proposed surveillance requirement would extend calibration of the inlet header and tube outlet thermocouples from an annual interval to a five year interval . We do not find this surveillance interval extension acceptable since no justification has been provided. 10U. Draft Item 3/4.6.3 - PCRV Liner Cooling System Temperatures No surveillance requirements comparable to SR 5.4.4 are given in this Draft Item. Consideration should be given to providing similar require- ments in the upgraded technical specifications. 11. SR 5.4.5 - PCRV Cooling Water System Flow Instruments Surveillance The proposed surveillance would extend annual calibration of the flow scanner instruments and alarms and the six subheader flowmeters to the next scheduled plant shutdown if they were not calibrated during the previous year. We find this extension acceptable up to a surveillance interval not exceeding 18 months since the potentials for additional plant transients are reduced and since the LWR-STS, in general , specifies surveillance intervals not to exceed 18 months when utilizing intervals of shutdown or refueling. - 21 - 11U. Draft Lem 3/4.6.2 - PCRV Liner Cooling System No surveillance requirements comparable to SR 5.4.5 are given. We believe that similar requirements should be considered in the upgraded technical specifications. 12. SR 5.5.3 - Reactor Building Exhaust System Surveillance e) The proposed surveillance requirement would verify at weekly intervals that the total pressure drop across the HEPA filter and charcoal absorber banks to be less than six inches of water at filter design flow ± 10 percent. Subsequent to this proposal the Draft Upgrade Technical Specifications have been issued and it is our opinion that appropriate portions of Draft Item 4.6.5.2.c.3, "Reactor Building Exhaust System," which generally specifies the testing requirements given in the Standard Technical Specifications, should be utilized in lieu of PSC's proposal . f) The proposed surveillance requirement would verify annually the performance capability and mechanical condition of each exhaust fan or at the next scheduled shutdown if such verification was not performed during the previous year. We find this surveillance requirement acceptable provided that the surveillance interval does not exceed 18 months , since the LWR-STS, in general , specifies surveillance intervals not to exceed 18 months when utilizing intervals of shutdown or refueling. - 22 - g) The proposed surveillance would require calibration of the instrumentation associated with the filters and fans at annual intervals or at the next scheduled shutdown if calibration was not performed during the previous year. We find these surveillance requirements are acceptable up to a surveillance interval not exceeding 18 months since the potentials for additional plant transients are reduced and since the LWR-STS, in general , specifies surveillance intervals not to exceed 18 months when utilizing intervals of shutdown or refueling. 12U. Draft Item 4.6.5.2 - Reactor Building Exhaust System The surveillance requirements described herein are generally consistent with LWR Standard Technical Specifications. However, additional infor- mation should be provided addressing: (1) Why there is no provision for vibration monitoring of the fans and for calibration of the exhaust system instrumentation and (2) Why should not the surveillance frequency be at 720 hour intervals rather than semi-annually? 13. SR 5.7.2a - Fuel Storage Facility Surveillance The proposed surveillance would require an annual functional test of the emergency ventilation system. This surveillance, together with parts a and b of SR 5.7.2c, have been substantially revised in Draft Item 4.9.3, "Fuel Storage Well ." We believe action on this item should be deferred until discussions on comment 13U. below are completed. - 23 - 13U. Draft Item 4.9.3 - Fuel Storage Well The material in this Draft Item appears to represent an improved and better developed surveillance than that described in SR 5.7.2 and should be considered for inclusion in SR 5.7.2a. - 24 - REFERENCES 1. 0. R. Lee (PSC) letter to J. T. Collins, "Proposed Technical Specification Changes - Inservice Inspection and Testing Requirements," No. P-83416, December 30, 1983. 2. Safety Evaluation by the Division of Reactor Licensing, U.S. Atomic Energy Commission in the Matter of Public Service Company of Colorado, Fort St. Vrain Nuclear Generating Station, Docket No. 50-267, January 30, 1972. 3. J. K. Fuller (PSC) letter to S. A. Varga, "Fort St. Vrain Inservice Inspection and Testing Program," No. P-79289, November 30, 1979. 4. P. C. Wagner (NRC) letter and enclosure to 0. R. Lee (PSC) , "Fort St. Vrain Nuclear Generating Station, Amendment No. 33 to Facility Operating License DPR-34," March 8, 1983. 5 0. R. Lee (PSC) letter to E. H. Johnson (NRC) , "Technical Specification Upgrade Program," December 20, 1984. SSINS No. : 6835 IN 85-73 UNITED STATESNU GELD OFFICECOFAR REGULATORY COMMISSION INSPECTIONANDENFORCEME i n POtro Y� p�l`'��0,T.C WASHINGTON, D. C. 20555 '( \ ; "iL, :') 111 August 23, 1985 SEP 31985 '' ' GH _ IE INFORMATION NOTICE NO. 85-73: EMERGENCY DIESEL GENERATOR C0NTPOL-EIRCUTT LOGIC DESIGN ERROR Addressees: All nuclear power reactor facilities holding an operating license (OL) or a construction permit (CP). Purpose: This information notice is to alert recipients of a potentially significant emergency diesel generator (EDG) control logic error that could prevent trans- fer to the emergency bus while the EDG is in the "maintenance shutdown" mode. It is expected that recipients will review the information for applicability to their facilities and consider actions, if appropriate, to preclude a similar problem occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements; therefore, no specific action or written response is required. Description Of Circumstances: According to the design, the EDGs at Rancho Seco Nuclear Power Generating Station enter the maintenance shutdown control mode whenever they are normally shut down from the control room or the remote EDG control panel . On June 1, 1985, the plant was shut down for refueling, an EDG was in the maintenance shutdown control mode after being secured from an operational condition (idling at 600 rpm with the output breaker open) , when an emergency bus was de-energized for planned work on a parallel bus. This created an undervoltage condition equivalent to a loss of offsite power (LOOP) on the emergency bus. The diesel generator sped up to the design speed but the EDG output breaker continuously cycled open and closed, thereby rendering the EDG set inoperable. Investigation by the licensee indicates that the cycling of the EDG output breaker was the result of a design error in the EDG control circuit logic. According to the licensee, the design 'deficiency affects proper response of the EDG set when it is operating in the maintenance shutdown control mode. Normal surveillance testing would not discover the control circuit design error because surveillance is not done in the maintenance shutdown control mode. The June 1, 1985 event at Rancho Seco represents the first time in the life of the plant that an undervoltage signal occurred with an EDG in the maintenance shutdown control mode. 8508210321 IN 85-73 August 23, 1985 Page 2 of 2 When an EDG is secured from operation, the control circuit logic places it in the maintenance shutdown control mode. In this mode, the control logic opens its output breaker and reduces its speed from 900 to 600 rpm. The EDG then idles at 600 rpm for 15 minutes before coasting down to rest. If a LOOP should occur while an EDG is in the maintenance shutdown control mode, the undervoltage signal causes it to speed back up to 900 rpm and to close its output breaker. This would cause the undervoltage signal to drop out. However, the maintenance shutdown control mode does not drop out for 30 seconds after the receipt of the undervoltage signal because of the control circuit design error. Thus, the maintenance shutdown control logic senses that the EDG output breaker is closed, opens the breaker, and resets the 15-minute timer for the maintenance shutdown control mode. As soon as the EDG output breaker opens, the undervoltage signal recurs and the EDG output breaker closes in response to the LOOP. The EDG output breaker continues to cycle open and closed as this process repeats itself. At Rancho Seco, this control circuit logic design error has been corrected by installing a relay to de-energize the maintenance shutdown control logic immediately upon receipt of an undervoltage signal . The Rancho Seco plant utilizes General Motors (GM) Model 20-465-E4 diesel generators with a 2750 kw nameplate rating. According to the licensee, the design error was in the interface provided by the Architect-Engineer (Bechtel) to the shutdown control logic provided by GM. Bechtel has advised the NRC that the Rancho Seco diesel generator control logic is unique and other plants designed by them are not affected. No specific action or written response is required by this information notice. If you have any questions about this matter, please contact the Regional Administrator of the appropriate regional office or this office. 'PdwardL. Jordan, Director Division, of Emergency Preparedness and En4ineering Response Office of Inspection and Enforcement Technical Contact: W. Swenson, NRR (301) 492-7876 R. Singh, IE (301) 492-8985 Attachment: List of Recently Issued Information Notices Attachment 1 IN 85-73 August 23, 1985 LIST OF RECENTLY ISSUED IE INFORMATION NOTICES Information Date of Notice No. Subject Issue Issued to 85-72 Uncontrolled Leakage Of 8/22/85 All power reactor Reactor Coolant Outside facilities holding Containment an OL or CP 85-71 Containment Integrated Leak 8/22/85 All power reactor Rate Tests facilities holding an OL or CP 85-70 Teletherapy Unit Full 8/15/85 All material Calibration And Qualified licensees Expert Requirements (10 CFR 35. 23 And 10 CFR 35.24) 85-69 Recent Felony Conviction For 8/15/85 All power reactor Cheating On Reactor Operator facilities holding Requalification Tests an OL or CP 85-68 Diesel Generator Failure At 8/14/85 All power reactor Calvert Cliffs Nuclear facilities holding Station Unit 1 an OL or CP 85-42 Loose Phosphor In Panasonic 8/12/85 Materials and fuel Rev. 1 800 Series Badge Thermo- cycle licensees luminescent Dosimeter (TLD) Elements 85-67 Valve-Shaft-To-Actuator Key 8/8/85 All power reactor May Fall Out Of Place When facilities holding Mounted Below Horizontal Axis an OL or CP 85-66 Discrepancies Between 8/7/85 All power reactor As-Built Construction facilities holding Drawings And Equipment an OL or CP Installations 85-65 Crack Growth In Steam 7/31/85 All PWR facilities Generator Girth Welds holding an OL or CP OL = Operating License CP = Construction Permit Hello